I couldn't help the laugh icon.... My friend Fred got ultra-precision ballscrews on his 10X50 mill, and he doe curse them from time to time. He had slowed down using it these days, so it is more frequent that he forgets to lock Y.... He and I laugh when it happens!
Nice that you managed the save! That is one powerful machine!
I just got a set of 5c collets, mine are not Accusize though, Findmall brand. Acceptable for the kind of halfassed precision work i was doing, but not great.Anyone have this set of Accusize 5c collets? I'd like to try them but import collets make me nervous.
Nice repair.... And another great reminder why I love my old trucks....... Taking the cab off to perform some engine work, I remember when those were found under the hood, in the engine compartment.....I'm working on a 2002 Ford F550 in the shop. I had to lift the cab off the frame for some engine work. Had trouble with the cab mounts. The nut plates are so rotten that the threads fell apart when I went to bolt them back up. The fix is longer bolts to go all the way through and put nuts on the bottom. One cab bolt is a special bolt that has a fat shank for body alignment. Here's what I did to make it 1.5" longer.
The mount looking up from the floor. Those are supposed to be threads inside.
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The special bolt:
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Parted off the 12mm threaded section:
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Tapped for 1/2" 13:
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Screwed in a chunk of allthread:
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Now it can pass all the way through the mount and get a nylock nut and flat washer.
Yeah, how sick & twisted was that?I remember when those were found under the hood, in the engine compartment...
Nicely done! You deserve a pat on the back for that innovative solution.Another interesting project tonight. Working on a 2018 Hyundai Elantra 1.8L engine. It came to me as a no start. Found that the exhaust camshaft was not turning. The timing chain was intact, so I pulled the cover and the timing gear/cam phaser. The pin that aligns and drives the cam had walked deeper into its bore in the cam.
I have seen this before, while working at the dealership. We would replace the cam and gear and send it out. I am unaware if they fixed the issue of the bore being deeper than the length of the pin, so I decided to see about fixing this one on my own.
The pin is 4.815 mm in diameter. I extracted it and replaced it with a broken tap shank that was slightly larger at 4.91 mm that I'd been saving for such an occasion.
Here's some pics:
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You can see that the pin walked in till it was flush.
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Some minor damage to the mating bore in the phaser.
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I pulled the cam and wrapped it up for some welding. Welded a 5mm washer to the pin, then a 10-24 machine screw with a nut to pry against. It came out very easy.
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Cleaned up the broken tap by slicing it off , and tapped it in with some loctite, until it was bottomed out.
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I'll trim it off to the proper length tomorrow and reassemble everything. I may bore and install a bushing in the gear,, but i don't think I will have to.